Sorry for being MIA.
I've been quite busy with working extra days at my 2nd job and helping the GF get her farmers market business going. I hadn't had much time to work on the Mustang.
I did get the front brake rotors for the 5-lug swap. So maybe I can start on that soon.
Baer 2 piece 13" rotors.
I had also been having a problem with the car stumbling/backfiring and then eventually shutting down.
So I decided to go ahead and do the 3G 130amp alternator install since I already had it.
I managed to get enough time to pull the old alternator and bracket off. Then I clearanced the bracket for the 3g alternator, and shot it with some paint.
Installed and wired the alternator up as well as cleaned up some of the wiring from the solenoid to the headlights and alternator.
That still didn't take care of the problem with the stumble and dieing. But it did mark off one of the items on the to do list. And I don't have to worry about low voltage when the electric fan is running.
I was able to manage to pull some codes and it came back as a PIP code. So ordered and installed a new distributor.
Since the current race and show season has been delayed, I decided to pull the upper intake and install the BBK fuel rails, Russell fuel lines, 24# Ford Racing injectors, and the Aeromotive fuel regulator.
But upon priming the system, there was a bad fuel leak between the rail and the regulator adaptor block. I tried to fix the leak 3 separate times to no avail. The design only has an O-ring sandwiched between the non-machined rail and the block with just 2 small screws to distribute the clamping pressure. To me this is a terrible design and I was not going to trust it.
So I ordered a set of Trick Flow black anodized rails, lines, and AN fittings.
I might paint the upper intake while it's off and clean up under the hood some. Maybe reroute vacuum lines and remove the ones that aren't being used. And possibly reroute and tuck some of the passenger side wire harness.